lunes, 25 de junio de 2012
¡ES EL AEROPUERTO, ESTÚPIDO!
Recordamos unos párrafos del Informe técnico A032-2008, informe final, publicado en Julio de 2011 por la Comisión de Investigación de Accidentes e Incidentes de Aviación Civil (CIAIAC)sobre el accidente del vuelo JK5022 de Spanair que tuvo lugar en el Aeropuerto de Madrid-Barajas el día 20 de agosto de 2008.
1. INFORMACIÓN SOBRE LOS HECHOS
1.1 Antecedentes del vuelo
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Una vez que despegó la aeronave inmediatamente anterior, a las 14:23:09 h Control (DEP) comunicó: «SPANAIR 5022 VIENTO 210 05 AUTORIZADO A DESPEGAR, PISTA 36 IZQUIERDA». La tripulación colacionó a las 14:23:14 h: «AUTORIZA A 36 IZQUIERDA SPANAIR EHHHH 5022».
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Durante la carrera de despegue se oyeron los anuncios en voz alta (call outs) «SIXTY», «ONE HUNDRED», «V1», «POWER CHECK» y «ROTATE14». En el momento en que se oyó «V1» la velocidad15 grabada en el DFDR fue de 154 KCAS y al oírse «ROTATE» se registró una velocidad de 157 KCAS.
A las 14:24:10 h en el DFDR quedó registrado el cambio de la señal de modo tierra a modo vuelo procedente del sistema de sensación de tierra de la pata de morro. La carrera de despegue tuvo una longitud aproximada de 1.950 m.
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A las 14:24:14 h se activó la vibración de la palanca de control del sistema avisador de pérdida (stall warning stick shaker) y la bocina y la voz sintética de aviso de pérdida simultáneamente. El copiloto dijo «FALLO DE MOTOR» en tono interrogativo y un segundo más tarde, a las 14:24:15 h el comandante, en un tono de voz muy elevado, preguntó cómo se apagaba la voz. En ese momento la velocidad era de 168 KCAS, había 25 ft de radio altura, un ángulo de asiento (pitch) de 15,5° y un alabeo (bank) a la derecha de 4,4°.
El alabeo a la derecha se incrementó hasta un máximo de 20°. En este momento quedó registrada una variación de la posición de las palancas de empuje de unos 4° la izquierda y 32° la derecha, en el sentido de disminuir el empuje, durante un segundo.
Como consecuencia de ello, el valor de EPR se redujo dos segundos después a un valor en torno a 1,65 en ambos motores, observándose variaciones de los parámetros de motor. Inmediatamente las palancas se movieron hasta su posición más adelantada posible, alcanzándose unos valores de EPR en torno a 2,20. Estos valores se mantuvieron constantes hasta el final.
A partir de ese momento se escucharon los avisos de «bank angle» procedente del sistema de aviso de proximidad al terreno (EGPWS) y en cabina sonaron alternativamente en tres (3) ocasiones la bocina y la voz sintética anunciando la condición de pérdida: «[bocina]stall, [bocina]stall, [bocina]stall», a veces solapados con el aviso del EGPWS. La vibración de la palanca de control del sistema avisador de pérdida permaneció activa hasta el primer impacto con el suelo.
A las 14:24:19 h se alcanzaron los máximos valores de ángulo de asiento (18,3°) y de radio altura (40 ft). A las 14:24:24 h se escuchó el primer impacto contra el terreno alcanzándose una aceleración vertical de 3,17 g. En ese momento la actitud registrada de la aeronave era de 10,4° de pitch y 5,3° de alabeo a la derecha. La velocidad era de 154 KCAS.
A las 14:24:30 h finalizó la grabación de datos de vuelo en el DFDR.
A 14:24:36 h una aeronave comunicó a Torre en frecuencia de Rodadura Central-Sur (GND C-Sur), que acababa de haber un accidente.
La aeronave acabó destruida a consecuencia de los impactos con el suelo y el incendio posterior.
3.2. Causas
La CIAIAC ha determinado que el accidente se produjo porque:
La tripulación perdió el control del avión como consecuencia de la entrada en pérdida inmediatamente después del despegue, por no haber configurado el avión correctamente, al no realizar la acción de despliegue de los flaps/slats, tras una serie de fallos y omisiones, junto con la ausencia de aviso de la configuración incorrecta de despegue.
La tripulación no identificó los avisos de pérdida ni corrigió dicha situación después del despegue —retrasó momentáneamente las palancas de potencia del motor, aumentó el ángulo de asiento y no corrigió el alabeo— produciéndose un deterioro de la condición de vuelo en pérdida.
La tripulación no detectó el error de configuración al no utilizar adecuadamente las listas de comprobación que contienen los puntos para seleccionar y comprobar la posición de flaps/slats en las labores de preparación de vuelo, en concreto:
• No llevó a cabo la acción de seleccionar flaps/slats con la correspondiente palanca de mando (en «After Start Cheklist»);
• No realizó la comprobación cruzada de la posición de la palanca y el estado de las luces indicadoras de flaps y slats al ejecutar la lista de comprobación «After Start»;
• Omitió la comprobación de flaps y slats en el punto «Take Off Briefing» de la lista de comprobación de taxi;
• En la comprobación visual realizada en la ejecución al punto «Final Items» correspondiente a la lista «Take Off Inminent» no se realizó una confirmación real de la posición de los flaps y slats, tal como mostraban los instrumentos de la cabina de vuelo.
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Y también unos párrafos del Informe definitivo del incidente del MD-83 de Mapjet acontecido el 5 de junio de 2007 en el Aeropuerto de Lanzarote.
1. INFORMACIÓN factual
1.1 Historial del vuelo
1.1.2. Vuelo Lanzarote-Barcelona
El despegue desde Lanzarote se produjo a las 10:45 hora local, desde la pista 03 utilizando “autothrottle”. El piloto a los mandos era el copiloto. Después de la rotación, que se realizó a una velocidad aproximada de 145 kt, se activó el “stick shacker” y la aeronave empezó a alabear a la izquierda y derecha hasta alcanzar ángulos de 63º al lado derecho y 60º al izquierdo. El comandante retrajo el tren de aterrizaje aprox. 25 a 30 segundos después del despegue mientras la aeronave continuaba oscilando a ambos lados del eje longitudinal. La aeronave continuó alabeando hasta alcanzar una velocidad superior a 200 kt.
La aeronave ascendió hasta 5.000 ft y la tripulación, en un primer momento, decidió continuar con el vuelo, decisión que rectificó inmediatamente y la aeronave regresó a Lanzarote. La tripulación no declaró emergencia. El aterrizaje se realizó normalmente sin que existiera incidencia.
No se produjeron daños ni a personas ni a la aeronave. El desembarque del pasaje se realizó con normalidad.
Y esto es lo que ocurrió el 20 de marzo de 2009 en Melbourne: Un A-340 de Emirates Airlines que realizaba el vuelo de Melbourne a Dubai se golpeó con la cola en la pista durante el despegue, y no remontó el vuelo hasta que sobrepasó el final de la pista 16 del Aeropuerto de Melbourne por la noche y con visibilidad normal.
Ninguno de los 275 ocupantes sufrió ningún daño; el avión sí, en la parte baja trasera del fuselaje. También resultaron afectados algunos elementos del final de pista.
Tres accidentes y dos resultados. El viento salvó al Mapjet de Lanzarote y un diseño adecuado salvó a los 275 pasajeros del A-340 en Melbourne. En Barajas el viento lanzó al JK5022 contra el suelo y errores de diseño del aeropuerto lo despeñaron por un barranco que aún despide a los vuelos que despegan en configuración norte. Desgraciadamente, el JK55022 no intentó el despegue desde Lanzarote o desde Melbourne.
¿Hay quién todavía cree que la culpa fue del relé? No, la culpa fue del aeropuerto. Sin dudarlo, una nueva investigación que contemple todos los aspectos concurrentes es necesaria.
Porque esto es lo que pensamos de la CIAIAC, al menos por lo que respecta a su informe sobre el accidente de Barajas del 20 de agosto de 2008.
Adjuntamos el informe publicado en SKYbrary.
A340 Overrun on Take Off
Source: www.skybrary.aero
The ATSB has published the final report into the March 2009 tail strike and runway overrun by an Airbus A340-500, caused by insufficient thrust having been set because of incorrect flight crew data entry in performance calculations.
A345, Melbourne Australia, 2009 (RE HF)
Category: Accidents and Incidents
Description
On 20 March 2009 an Airbus A340-500 being operated by Emirates Airline on a scheduled passenger flight from Melbourne to Dubai with an augmented (relief) crew occupying the two flight deck observer seats suffered a tail strike and did not become airborne until after the end of take off runway 16 at Melbourne at night in normal ground visibility. Only subsequently, when an ECAM (Electronic Centralized Aircraft Monitoring) annunciation of a tail strike was apparent and ATC called, did the crew realise that a tail strike and overrun had occurred and it was decided to return to land to “assess the damage” with a ‘PAN’ was subsequently declared. An unusual noise accompanied by a cabin report of smoke in the rear cabin area just after completion of fuel dumping led to a precautionary request to ATC for a landing as soon as possible but a full inspection after coming to a stop on the runway founds no signs of fire and a normal taxi in to a gate was then made for disembarkation. None of the 275 occupants were injured but the aircraft rear lower fuselage and ground installations beyond the end of the departure runway struck by it were damaged.
Investigation
An Investigation was carried out by the Australian Transport Safety Bureau (ATSB). FDR data recording was found to have ceased as the aircraft had become airborne and this was attributed to the dislodgement of the FDR from its mounting rack immediately behind the rear pressure bulkhead to where it was found after the flight, lying (undamaged) on the lower fuselage skin below and slightly to the rear of the mounting rack. Fortunately, a DAR (Digital ACMS Recorder) was also fitted and had recorded most of the FDR parameters as well as others in Non-Volatile Memory (NVM).
The trajectory of the aircraft during the take off was established from the evidence available. The aircraft rear lower fuselage had contacted the 3657 metre long runway at three locations, starting at 265 metres, 173 metres and 110 metres from the end of the runway. It had then overrun the end of the runway onto the stopway and across the grassed clearway, becoming airborne three seconds after the selection of TOGA thrust. However, before gaining altitude, the aircraft had struck a Runway 34 lead-in sequence strobe light and several antennae, the latter impacts having disabled the Runway 16 ILS. A small depression at the end of the 60 metre stopway had resulted in the rear fuselage briefly losing contact with the ground and the final ground contact mark had ended 148 metres beyond the end of the paved runway surface (and beyond the 120 metre Clearway).
Figure 1 - Graphical representation of Digital Aircraft Condition Monitoring System Recorder (DAR) data showing position of aircraft at a computed airspeed corresponding to V1 used by the crew, initial tail contact with ground, and final tail ground contact witness mark. Source: ATSB AO-2009-012 Final Report.
Inspection of the aircraft lower rear fuselage found the lower skin to have been abraded by contact with the runway surface and in some areas worn through its full thickness with grass and soil caught in the airframe structure. One service panel had been dislodged and was subsequently found beyond the end of the take off runway along with numerous pieces of metal from the abraded skin panels.
It was established that performance calculations for the take off had been made using the Airbus Less Paper Cockpit (LPC) system on a single EFB. In accordance with the Operator’s SOP, the second EFB carried was used only as a backup in the event of a malfunction in the one being used. An aircraft take off weight of 100 tonnes less than the actual weight available to the flight crew was inadvertently entered into the EFB and the effects of that error on speeds and thrust settings were not subsequently noticed by any of the four pilots present. When the aircraft failed to become airborne after two ‘Rotate’ calls using the reduced thrust calculated, the aircraft commander had applied TOGA thrust and a few seconds later the aircraft had become airborne. Whilst still airborne, the crew had established for themselves the origin of the difficulty getting airborne as the gross error in the entered take off weight when the EFB was accessed to begin the landing performance calculations.
The Investigation found that there had been a complete failure of the procedural cross checks to detect the gross error of weight or its effects. The operating First Officer, who had also been PF for the take off, was found to have made the initial weight input error and the required cross check by the aircraft commander of the take-off weight in the FMGS with that used in the take-off performance calculation was then not made. The aircraft commander had entered the EFB performance figures into the FMGS and crosschecked them with the First Officer against the erroneous values that had previously been copied onto the flight plan. He had then handed the EFB back to the First Officer, who had stowed it before they completed the loadsheet confirmation procedure together. During that procedure, it was found that the First Officer had correctly read the weight from the FMGS as 361.9 tonnes but, when reading the same weight from the flight plan, had stated 326.9 tonnes before immediately correcting this to 362.9 tonnes. This procedure also included the First Officer reading out the (wrongly recorded) ‘green dot speed’ (best speed for climb once clean, affected only by aircraft weight and altitude) of 265 knots (490.78 km/h, 136.21 m/s) from the FMGS which was accepted by the aircraft commander.
During the take off roll, using an assumed temperature calculation of reduced thrust which had been produced using the wrong (low) take off weight, the rate of acceleration had not been perceived as lower than required. The rotation rate used was found to have been as prescribed and the tail strike had been the result of continued rotation following the second ‘rotate’ call which led to the aircraft reaching the geometric limit of 9.5° after which TOGA thrust was applied. It was considered “unlikely that the flight crew had time to recognise that the aircraft had not lifted off at the expected pitch attitude of about 8°.” In this respect, it was noted that, at the prevailing rotation rate, it would have taken only about half a second to increase the pitch by 1.5°, making the PFD an ineffective means of identifying the exceedence.
It was noted that, whilst climbing to 7000 feet2,133.6 m to commence fuel dumping, it had become apparent that the aircraft was not pressurising. No specific reason could be established for the apparent sight and smell of smoke in the rear cabin that had accompanied it but it was considered that the change in aircraft attitude as descent was commenced probably led to dust and odours from the earlier damage.
The Investigation distinguished two aspects of the accident as:
• the over rotation which led to the tail strike
• the long take off roll which led to the overrun
The Investigation examined in detail the ways in which a number of cross checks built in to the procedures for establishing take off data had all failed. The “lack of recognition of the degraded take off performance (relative to that needed) until very late in the take off run” was considered to have compounded the use of erroneous take off data which had created the conditions for the accident. However, it was noted that pilots rated for mixed fleet operations, as in this case for the A330-200, A340-300 and A340-500, there was an exposure to a large range of take off weights and (perceived) accelerations. Given that distraction was considered to have played a major part in facilitating error, a detailed examination of the effectiveness of risk management in this area was made. It was considered that:
• The operator had identified other flight phases as critical to the safety of flight, such as taxi, takeoff and climb, and had a sterile cockpit rule for those phases. There was no such management practice to reduce the potential for distraction during the take-off performance calculation and checking process.
• The provision by the operator of briefings to flight crews on distraction management in the months prior to the accident appear to have been ineffective in this accident.
In respect of the augmenting crew, it was considered that:
• The lack of clear direction on the role of, and required input from the augmenting crew during the pre-departure preparation further increased the distraction risk to the operating flight crew.
• The presence of augmenting crew in the cockpit during the pre-departure phase (in itself) created a distraction for the operating crew.
In respect of the SOPs involved, there was concern that, as usual, they were “typically designed on the basis that information flow….is sequential and....procedures are conducted in a linear fashion based on this sequential information flow” whereas research has shown such a linear flow is atypical in line operations which “increases the likelihood that, following a distraction, the flight crew will re-enter a procedure at an incorrect point.”
It was concluded after eliminating all other possible causes and establishing the chain of events with all the available evidence that “the over rotation and tail strike were due to the incorrect rotation speed and flap configuration for the actual weight of the aircraft”.
The preface to the Findings included the remarks that “although there are a number of factors identified directly relating to this accident, the accident needs to be taken in the context of the long history of similar take-off performance events.” Consequently, the recommended safety responses as result of the Investigation are “those that address the whole situation, not just those that address the specific factors identified in this accident”.
Five Safety Issues were identified:
• The existing take-off certification standards, which were based on the attainment of the take-off reference speeds, and flight crew training that was based on the monitoring of and responding to those speeds, did not provide crews with a means to detect degraded take-off acceleration. [Significant safety issue]
• The operator’s training and processes in place to enable flight crew to manage distractions during the pre-departure phase did not minimise the effect of distraction during safety critical tasks. [Significant safety issue]
• The available Cross Crew Qualification and Mixed Fleet Flying guidance did not address how flight crew might form an expectation, or conduct a ‘reasonableness' check of the speed/weight relationship for their aircraft during takeoff. [Significant safety issue]
• The failure of the digital flight data recorder (DFDR) rack during the tailstrike prevented the DFDR from recording subsequent flight parameters. [Minor safety issue]
• The lack of a designated position in the pre-flight documentation to record the green dot speed precipitated a number of informal methods of recording that value, lessening the effectiveness of the green dot check within the loadsheet confirmation procedure. [Minor safety issue]
Safety Action in response to the accident and the investigation of it by the ATSB itself in initiating and completing a Safety Study on “Take-off performance parameter errors: A global perspective” was noted. After taking account of Safety Action by Emirates, Airbus, EASA and FAA as described in the Report, the ATSB made one Safety Recommendation:
• That the FAA take action to address the existing take-off certification standards, which are based on the attainment of the take-off reference speeds, and flight crew training that was based on the monitoring of and responding to those speeds, and do not provide crews with a means to detect degraded take-off acceleration. (AO-2009-012-SR-079)
In respect of the outstanding concern about the issues raised by ‘Cross Crew Qualification and Mixed Fleet Flying’ the Investigation determined that the best way to progress this matter was to direct ‘Safety Advisory Notices’ to the FSF and to IATA requesting respectively that:
• The Flight Safety Foundation consider developing guidance to assist flight crews form appropriate mental models in respect of the weight and corresponding take-off performance parameters for a particular flight. The use by operators of mixed fleet flying increases the importance of that guidance. (AO-2009-012-SAN-086)
• The International Air Transport Association to encourage its members to develop guidance to assist their flight crews form appropriate mental models in respect of the weight and corresponding take-off performance parameters for a particular flight. The application by operators of mixed fleet flying increases the need for that guidance. (AO-2009-012-SAN-087)
The Final Report of the Investigation was published on 16 December 2011: Aviation Occurrence Investigation AO-2009-012 Final.
Related articles and further readings were not included but are available in the skybrary article.
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1 comentario:
En primer lugar mi más sincera felicitación al equipo de Las Mentiras de Barajas, sobretodo por la comparación ente el accidentente de Barajas y el incidente de Lanzarote, en dos aeropuertos españoles, que lo dice todo.
En segundo lugar una matización muy importante, fueon dos accidentes y un incidente y encima este ocurrido un año y pico antes que el accidente de Barajas.
En tercer lugar algunos detalles desde el punto de vista técnico, no todos porque son muchísimos, para que se puedan contemplar en un artículo tan reducido.
1.- Al abrir este artículo con; "Recordamos unos párrafos del Informe técnico A032-2008, informe final, publicado en Julio de 2011 por la Comisión de Investigación de Accidentes e Incidentes de Aviación Civil (CIAIAC)sobre el accidente del vuelo JK5022 de Spanair que tuvo lugar en el Aeropuerto de Madrid-Barajas el día 20 de agosto de 2008.",
considero que se le debía haber añadido; ,
un año y pico despues del incidente del MD-83 de mapjet en Lanzarote, y terminando con;
¿Para que sirve el punto 6.5 del Anexo 13 de OACI y por tanto la CIAIAC que pagamos entre todos los españoles?
2.- ¿Por qué en el informe sobre el incidente de Lanzarote, aunque se efectúa más de dos años después y desgraciadamente ya no sirvio para nada, la CIAIAC omite poner el dato sobre cual era el viento con el que fue autorizado a despegar por la pista 03 de Lanzarote, máxime cuando los pilotos que están vivos habían declarado que consiguieron despegar gracias al BUEN VIENTO DE CARA?
3.- Las Mentiras de Barajas deberían hacer publico del Informe de la CIAIAC sobre el incidente de Lanzarote, que la entrada en perdida durante el despegue se agravó considerablemente al subir indebidamente en este caso el tren de aterrizaje, porque la subida del tren conlleva la subida y el cierre de las compuertas del alojamiento del tren de aterrizaje
Por último y termino, no sin antes de hacrle la siguiente sugerencia al equipo de Las Mentiras de Barajas;
Este artículo se lo deberían de remitir por un lado al Juez Decano de Madrid, D. Jose Luis Armengol, que con todo el acierto del mundo y más preguntaba si la pista 36L de Barajas aquel fatídico día del 20 de agosto de 2008 era o no apta para el despegue de un MD-82, es decir, cual era el Máximo Peso Permitido al Seapegue (PMTOW), y por otro lado a la EASA ahora que la han sido admitidas las más de 50,000 firmas presentadas por la Asociaciacion de Afectados del Vuelo JK5022 solicitándoles la reapertaura de un nuevo Informe.
Luis Guil
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